Notices
Drivetrain Gearbox, Diffs & Driveshafts etc

header tank made from biscuits :-(

Thread Tools
 
Search this Thread
 
Old 07 June 2002, 12:46 PM
  #1  
UkLegacyT
Scooby Regular
Thread Starter
 
UkLegacyT's Avatar
 
Join Date: Jan 2002
Posts: 1,909
Likes: 0
Received 0 Likes on 0 Posts
Post

just snapped the top hose off

i take it this is pressurised, and so no temporary fix?

cheers, ian
Old 07 June 2002, 12:49 PM
  #2  
David_Wallis
Scooby Regular
 
David_Wallis's Avatar
 
Join Date: Nov 2001
Location: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
Posts: 15,239
Likes: 0
Received 1 Like on 1 Post
Post

There was a guy on here advertising alloy ones... Can you drill a hole down the middle of a bolt and then bolt this in till you get another?

David
Old 07 June 2002, 12:51 PM
  #3  
UkLegacyT
Scooby Regular
Thread Starter
 
UkLegacyT's Avatar
 
Join Date: Jan 2002
Posts: 1,909
Likes: 0
Received 0 Likes on 0 Posts
Post

you again

yeah, ive got a hollow turbo water feed bolt here, so may just try that, you think it'll hold the pressure?

cheers mate
Old 07 June 2002, 12:54 PM
  #4  
David_Wallis
Scooby Regular
 
David_Wallis's Avatar
 
Join Date: Nov 2001
Location: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
Posts: 15,239
Likes: 0
Received 1 Like on 1 Post
Post

Its got two choices... I bit of epoxy.. Araldite around it as well...

Im not watching football, so got nothing better to do..

David
Old 07 June 2002, 12:56 PM
  #5  
UkLegacyT
Scooby Regular
Thread Starter
 
UkLegacyT's Avatar
 
Join Date: Jan 2002
Posts: 1,909
Likes: 0
Received 0 Likes on 0 Posts
Post

ah yes, ill get the epoxy resin out and find a bit of tube or something

whats happening with the front mount mate, seems to have slowed
Old 07 June 2002, 01:11 PM
  #6  
David_Wallis
Scooby Regular
 
David_Wallis's Avatar
 
Join Date: Nov 2001
Location: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
Posts: 15,239
Likes: 0
Received 1 Like on 1 Post
Post

Cant really be bothered at the moment... still trying to source a welder... Quite busy at the moment helping a mate decorate his house... then I can never be bothered when I get home from work..

David
Old 07 June 2002, 01:15 PM
  #7  
UkLegacyT
Scooby Regular
Thread Starter
 
UkLegacyT's Avatar
 
Join Date: Jan 2002
Posts: 1,909
Likes: 0
Received 0 Likes on 0 Posts
Post

youve done good so far anyway mate

ive only got the mig like you mate, otherwise would have helped.
mate had a tig, until it got robbed about a month back...£1500
scum
Old 07 June 2002, 01:50 PM
  #8  
David_Wallis
Scooby Regular
 
David_Wallis's Avatar
 
Join Date: Nov 2001
Location: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
Posts: 15,239
Likes: 0
Received 1 Like on 1 Post
Post

I knew I should have used steel pipe..

David
Old 07 June 2002, 02:46 PM
  #9  
ustolemyname??stevieturbo
Scooby Regular
iTrader: (1)
 
ustolemyname??stevieturbo's Avatar
 
Join Date: Mar 2002
Location: Norn Iron
Posts: 2,786
Likes: 0
Received 0 Likes on 0 Posts
Post

The header tanks are soft as ****. Forge do an alloy one I believe, but you will need deep pockets. Leak fix is a good repair Sleeve a bit of pipe into the tank then bond it in.. It is like chemical metal ( same manufacturer ) but designed for rad/fuel etc applications. It doesnt go soft when heated like some of the others do. I have seen these break with only the slightest touch. It is definately a weak point on the early cars. The radiator end tanks arent much better. Best to get a replacement for long term reliability.
Old 07 June 2002, 07:54 PM
  #10  
mrp
Scooby Regular
 
mrp's Avatar
 
Join Date: Jan 2002
Posts: 180
Likes: 0
Received 0 Likes on 0 Posts
Post

I did a temporary repair using a washing machine 90 degree hose connector, cut off the straight ribbed piece, wedged it in the hole that was left, sealed the whole lot with epoxy putty and reconnected the hose to it. There was no problem with the header being pressurised. I would have kept the tempory fix as there were no leaks but my nice friendly dealer replaced it under warranty.
Old 07 June 2002, 08:59 PM
  #11  
UkLegacyT
Scooby Regular
Thread Starter
 
UkLegacyT's Avatar
 
Join Date: Jan 2002
Posts: 1,909
Likes: 0
Received 0 Likes on 0 Posts
Post

hi guys, fixed it
used an end of the turbo water feed pipe (spare one), drilled out the hole enough and smacked it in, then used layers of epoxy resin.
give it a caning before, and touch wood, it seems ok

thanks, ian.
Old 07 June 2002, 10:03 PM
  #12  
Scott.T
Scooby Regular
iTrader: (2)
 
Scott.T's Avatar
 
Join Date: Feb 2000
Location: East Sussex
Posts: 6,181
Likes: 0
Received 1 Like on 1 Post
Post

They seem to be getting to that age, where these things are starting to go.

Mine went in Feburary, cost £60 for a new one from Suabaru.

Know what you mean about Biscuits, that damn things goes lke a cheap digestive and a cup of ovaltine.
Old 08 June 2002, 02:27 PM
  #13  
stratman
Scooby Regular
 
stratman's Avatar
 
Join Date: May 2000
Posts: 617
Likes: 0
Received 0 Likes on 0 Posts
Post

Mine went on m M96 ( before it got nicked )

I tried araldite, and various epoxies. I eventually got a metal STi one from Midland Impreza. Grade A Subaru also have em. I had to make a bit of a bracket out of steel plate to mount it.

Its the only long term solution cos the original equipment plastic tanks are crap.

The forge one is a nice polished ally but ridiculously expensive.
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Mattybr5@MB Developments
Full Cars Breaking For Spares
28
28 December 2015 11:07 PM
Mattybr5@MB Developments
Full Cars Breaking For Spares
12
18 November 2015 07:03 AM
Ganz1983
Subaru
5
02 October 2015 09:22 AM
IAN WR1
ScoobyNet General
8
28 September 2015 08:14 PM
shorty87
Other Marques
0
25 September 2015 08:52 PM



Quick Reply: header tank made from biscuits :-(



All times are GMT +1. The time now is 07:14 AM.