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VF28 not achieving boost target

Old Feb 24, 2005 | 10:45 PM
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Unhappy VF28 not achieving boost target

Help!! Have above turbo fitted to my98 uk. I have an apexi ecu with various boost settings mapped at 1-1.3bar. Problem is that the turbo is maxing out at 1bar even if the higher setting is selected. What would cause the turbo not to achieve its target?

Other mods on the car are full decat, sti4 tmic, green panel filter and uprated fuel pump.

One other thing i noticed today was that when engine was left idling for about 20 seconds and then switched off i could still hear the turbo spin for a couple of seconds after. Is this normal?

Thanks.

Bill.
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Old Feb 24, 2005 | 10:49 PM
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I cant help with the boost issue, but the VF series turbo's have roller bearings, rather than the sleeve type of the td0X turbos, so they do spin more freely. My VF22 can be heard spinning down even after a good cool down period.
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Old Feb 24, 2005 | 10:53 PM
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Originally Posted by bruce
I cant help with the boost issue, but the VF series turbo's have roller bearings, rather than the sleeve type of the td0X turbos, so they do spin more freely. My VF22 can be heard spinning down even after a good cool down period.
Thanks. Thats one less thing to worry about.
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Old Feb 24, 2005 | 11:02 PM
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do you have a samco inlet pipe fitted?
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Old Feb 24, 2005 | 11:06 PM
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Originally Posted by StickyMicky
do you have a samco inlet pipe fitted?
No. just the standard one.
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Old Feb 24, 2005 | 11:08 PM
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when you say the turbo is being maxed out what exactly do you mean?
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Old Feb 24, 2005 | 11:10 PM
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It reaches a peak of 1bar and no more. The ecu has been mapped for 1, 1.1, 1.2 and 1.3bar. When selecting 1.2 for eg, the turbo will still only peak at 1bar.
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Old Feb 25, 2005 | 02:09 PM
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bttt
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Old Feb 25, 2005 | 03:58 PM
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Last time i had my car mapped at Bob Rawle's a P1 had the same problem and would'nt boost over 1 bar, it turned out to be the plugs/coil pack were a bit duff.
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Old Feb 25, 2005 | 06:29 PM
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just in case- turbo off- and check for cracks near/around wastegate exhaust housing.

Happened to me for the last few months- didnt even realise.. until I got on an RR for mapping work.

New turbo in my case.
Old one going to be repaired.
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Old Feb 26, 2005 | 05:35 PM
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Could a faulty map sensor be the cause? A fault code has been thrown up of bst1 on apexi commander.
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Old Feb 26, 2005 | 06:52 PM
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Just had a drive with the pipe disconnected from the actuator, and max boost was 1.1bar in 3rd and 4th gears upto 4.5k in 3rd and 4k in fourth. Didnt push it any further. Any ideas to where problem may lie?

Thanks
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Old Feb 26, 2005 | 07:42 PM
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If thats the case then it sounds like you have a crack or a leak somewhere or maybe the turbo is worn out, they do not have the same life expectancy as the Td series turbo's

What chrome says is the best solution, pull it and have a good look around as only making 1 bar with the actuator removed is not good

AP
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Old Feb 26, 2005 | 07:49 PM
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the inlet air hose isnt collapsing at high boost is it? Check if it is rigid enough.
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Old Feb 26, 2005 | 08:54 PM
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It should immediately overboost with the pipe disconnected. In this case I'd suspect a fault with the turbo or wastegate actuator.

Andy
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Old Feb 26, 2005 | 11:10 PM
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my old turbo did exactly what yours is doing about 6 months ago, got a new turbo under warranty
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Old Feb 26, 2005 | 11:45 PM
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cheers guys. looks like a new turbo. andy i maybe calling you for one of your td05's.
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Old Feb 27, 2005 | 09:46 PM
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small note, my turbo is currently struggling to reach over 1bar

the recirc dumpvalve is jammed open and isnt giving a seal.
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Old Feb 27, 2005 | 11:06 PM
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Worth checking certainly
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Old Feb 28, 2005 | 01:14 AM
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Also check that the waste gate actuator is allowing the penny valve to fully close.
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Old Feb 28, 2005 | 12:25 PM
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I tried another standard dumpvalve that i had lying around, no change. But i will certainly check the wastegate now.

Thanks.
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Old Feb 28, 2005 | 07:03 PM
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i "sorted" my dumpvalve today to see sum small gains, but the gains were not nearly enough

with my dawse device fully wound in, its hitting about 1.15/1.20 bar peak boost and it will go no higher.

on the way home from reading yesterday while doing sum overtaking, boost was sitting at about .8bar or so most of the way home, when i went to overtake sumbody, i put my foot down to find the thing shoot off like it used to, next time i tried this the boost had dropped back down again

later on in the trip i over took sumbody with my foot flat down, as the revs climbed (as fast as they can with .8bar on a vf23) it suddenly started climbing to 1.2bar were it sat there till i backed off)

next time it was back down to .8bar

today i cleaned the dawse device and replaced the pipes for it, no change, only fully winding the dawse in, made the boost rise, although its still not as high as its supposed to

i have a spare actuator in the garage i will try out tomorrow, and report back.
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Old Feb 28, 2005 | 07:31 PM
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Originally Posted by StickyMicky
i "sorted" my dumpvalve today to see sum small gains, but the gains were not nearly enough

with my dawse device fully wound in, its hitting about 1.15/1.20 bar peak boost and it will go no higher.

on the way home from reading yesterday while doing sum overtaking, boost was sitting at about .8bar or so most of the way home, when i went to overtake sumbody, i put my foot down to find the thing shoot off like it used to, next time i tried this the boost had dropped back down again

later on in the trip i over took sumbody with my foot flat down, as the revs climbed (as fast as they can with .8bar on a vf23) it suddenly started climbing to 1.2bar were it sat there till i backed off)

next time it was back down to .8bar

today i cleaned the dawse device and replaced the pipes for it, no change, only fully winding the dawse in, made the boost rise, although its still not as high as its supposed to

i have a spare actuator in the garage i will try out tomorrow, and report back.
Mines only hit 1.15bar with the actuator pipe disconnected. Will try cleaning out all the pipes/hoses. One other thing i noticed was that there was oil in the pipe to the actuator.
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Old Feb 28, 2005 | 09:11 PM
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this is pretty strange!!

im going to nip out in mine for 5 mins with the pipe disconnected and see what it does !
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Old Feb 28, 2005 | 09:25 PM
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went for a quick spin

disconected my actuator from the dawse device and floored it, as it came on boost it shot up to 1.49bar about 3/4 times so i guess its the dawse device thats sumhow broke?

i only drove it just as it came on boost, my car fuel cuts at 1.45bar if its held for a few moments so i wasnt going to hold the throttle or do anything stupid like that.

i must have an air leak or sumthing on the dawse
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Old Mar 2, 2005 | 08:44 AM
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removed my dawse once again, cleaned it (was not dirty tbh) removed the IC and refitted and all is well.

hope you get yours sorted!
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Old Mar 2, 2005 | 04:14 PM
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Originally Posted by StickyMicky
removed my dawse once again, cleaned it (was not dirty tbh) removed the IC and refitted and all is well.

hope you get yours sorted!
No joy yet.
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