MY. 02 WRX ..... the story so far
#1
MY. 02 WRX ..... the story so far
Spec .
2002WRX
Motec M800 pro
USDM 2.5 sti block
wrx cams
polished heads
cp pistons block machined to fit new pistons
ballanced crank
900cc injectors
Trust FMIC
custom fuel rails (made by me)
custom equal length headers (me)
custom up pipe(me)
Tail 40mm ext waste gate
hybrid T61 turbo
fuel lines all changed to 9mm aero quip push on
2xwalbro 255,s in tank
erl water inj
there is mor i will remember later
drive train
cusco twin plate clutch
sti2 ger box fitted with PPG 3/4
quick shift
plated rear diff
open front diff
std drive shafts
std prop
tein coil overs
brembo gran turismo 330mm brake kit
wheels
Compomotive MO 8/18
yoko AVS sport 225/40/18
Exterior
C/F bonnet soon to go want std wr blue one back anyone.
C/F S202 rear spoiler swap for hi sti7/8 in wr blue
Interior
car came std with UK300 interior ble alcatera
PLX wide band
gredy boost guage
greddy egt
greddy oil press
sony head unit
well after 5k+ mils and 4 gear boxes it gave up the ghost and broke the ring lands
on 3 pistons on comp test No 2 was down to 75psi . but considering that this was done not as bad but quite bad when it went on rollers at well lane and did
421bhp not bad i supose .. well i finnished off the engine yesterday and up and running at 11pm last night .
i built the new engine with new pistons,bearings,turbo,
used Cometic 1.4mm head gaskets and std Subaru bearings
and CP pistons with new Subaru rings i have lots of other bitts to go on in time .
will up date as i go on ..... chris
2002WRX
Motec M800 pro
USDM 2.5 sti block
wrx cams
polished heads
cp pistons block machined to fit new pistons
ballanced crank
900cc injectors
Trust FMIC
custom fuel rails (made by me)
custom equal length headers (me)
custom up pipe(me)
Tail 40mm ext waste gate
hybrid T61 turbo
fuel lines all changed to 9mm aero quip push on
2xwalbro 255,s in tank
erl water inj
there is mor i will remember later
drive train
cusco twin plate clutch
sti2 ger box fitted with PPG 3/4
quick shift
plated rear diff
open front diff
std drive shafts
std prop
tein coil overs
brembo gran turismo 330mm brake kit
wheels
Compomotive MO 8/18
yoko AVS sport 225/40/18
Exterior
C/F bonnet soon to go want std wr blue one back anyone.
C/F S202 rear spoiler swap for hi sti7/8 in wr blue
Interior
car came std with UK300 interior ble alcatera
PLX wide band
gredy boost guage
greddy egt
greddy oil press
sony head unit
well after 5k+ mils and 4 gear boxes it gave up the ghost and broke the ring lands
on 3 pistons on comp test No 2 was down to 75psi . but considering that this was done not as bad but quite bad when it went on rollers at well lane and did
421bhp not bad i supose .. well i finnished off the engine yesterday and up and running at 11pm last night .
i built the new engine with new pistons,bearings,turbo,
used Cometic 1.4mm head gaskets and std Subaru bearings
and CP pistons with new Subaru rings i have lots of other bitts to go on in time .
will up date as i go on ..... chris
Last edited by wrrjones; 30 December 2004 at 01:00 PM.
#5
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Cheers Chris.
Curious.. did you leave the ext. wastegate vent open to atmosphere?
P.S. more pics please!!
Curious.. did you leave the ext. wastegate vent open to atmosphere?
P.S. more pics please!!
Last edited by AlanG; 30 December 2004 at 07:15 PM. Reason: addition
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#11
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Join Date: Nov 2001
Location: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
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Did you crack a ring land? what damage to the piston?
How do you think you damaged the ring lands??
David
How do you think you damaged the ring lands??
David
#12
David
ill post up pics of pistons 3 pistons with ringland failure 1 is realy bad other 2 are just bad
failure was down to too much boost i.e 2bar before 1.5 was fine when i removed the pistons the ringlands on 1 piston just fell out looked like they had been plasma cut lol...chris
Jon.
i like the FMIC seems to work well i have a new one in case .....chris
ill post up pics of pistons 3 pistons with ringland failure 1 is realy bad other 2 are just bad
failure was down to too much boost i.e 2bar before 1.5 was fine when i removed the pistons the ringlands on 1 piston just fell out looked like they had been plasma cut lol...chris
Jon.
i like the FMIC seems to work well i have a new one in case .....chris
#13
more pics
pics of 2 of the damaged pistons the cracked sections actually dropped out when i removed rings.
just have a couple of jobs left to do like re site the fuel filters still need a 2.5ins 45deg samco that should be here on tues lets see need some more exhaust wrap lol...
chris
Last edited by wrrjones; 02 January 2005 at 06:54 PM.
#15
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Location: All over the place, trying to stop putting the miles on!
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I don't know about cracking the ring lands, more like shattering them!!
Looks like you took a chisel to them
Dan.
P.S. Thanks for the peek under the bonnet in the que at the Pod, some good time u run that day too!
Looks like you took a chisel to them
Dan.
P.S. Thanks for the peek under the bonnet in the que at the Pod, some good time u run that day too!
#17
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One for anti lag.
Cant believe you went for the Red inlet after all esp after what that kid said at the pod
Rob
Cant believe you went for the Red inlet after all esp after what that kid said at the pod
Rob
Last edited by tweenierob; 03 January 2005 at 12:15 PM.
#20
Originally Posted by AlanG
{Interested} How does that work?
PM, if you don't want to fill up your project thread with my drivel. lol
PM, if you don't want to fill up your project thread with my drivel. lol
Alan
it acts like a hand throttle keeping the butterfly open at i.e 2500 rpm so on gear change the buttefly never shuts ie feeding the antilag ..... you want some more pics ???... chris
#21
Originally Posted by wrrjones
David
ill post up pics of pistons 3 pistons with ringland failure 1 is realy bad other 2 are just bad
failure was down to too much boost i.e 2bar before 1.5 was fine when i removed the pistons the ringlands on 1 piston just fell out looked like they had been plasma cut lol...chris
Jon.
i like the FMIC seems to work well i have a new one in case .....chris
ill post up pics of pistons 3 pistons with ringland failure 1 is realy bad other 2 are just bad
failure was down to too much boost i.e 2bar before 1.5 was fine when i removed the pistons the ringlands on 1 piston just fell out looked like they had been plasma cut lol...chris
Jon.
i like the FMIC seems to work well i have a new one in case .....chris
Carlos
#23
Carlos..
the rods arnt the problem and in inspection they were mint no probs at all the pistons wont take any more than 1.5 reliably and any one that exeeds that is looking for trouble ... was running 2.2 bar at one point when the pistons were poorly to see how everything stood up and every thing else was fine ran 2+ bar for 1000 mils maby more but the engine was breathing heavly by this time and i wanted to see how it went as i had spare short motor which was rebuilt with forged internals by me to slot in ...
Dyney
are you on 2.5 usdm sti?..
if so i would be realy carefull with std pistons and make sure you keep the boost down
if not take a look at my pistons ..... chris
the rods arnt the problem and in inspection they were mint no probs at all the pistons wont take any more than 1.5 reliably and any one that exeeds that is looking for trouble ... was running 2.2 bar at one point when the pistons were poorly to see how everything stood up and every thing else was fine ran 2+ bar for 1000 mils maby more but the engine was breathing heavly by this time and i wanted to see how it went as i had spare short motor which was rebuilt with forged internals by me to slot in ...
Dyney
are you on 2.5 usdm sti?..
if so i would be realy carefull with std pistons and make sure you keep the boost down
if not take a look at my pistons ..... chris
#25
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Join Date: Nov 2001
Location: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
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carlos has some good pics of his on 22b a while ago...
Motec also sell a throttle kicker for this.
David
Motec also sell a throttle kicker for this.
David
#26
yeah they do but i all ready had this one made by Apexi works well enoughand its realy sensitive so easy to make minor adjustments and 1 click off dont have to wind it back in ill get some more pics tomorrow of the set up inside the car as i will be out with the laptop lol as its been out for first run today the set up is tptally different to last one getting det at 0.5 bar lol.... ... chris
Last edited by wrrjones; 06 January 2005 at 08:13 PM.
#28
well been mapping and up to 1.5 bar atm and all going well cant beleve everything is so different on new eng from last build and mapping ,, ie pistons rods 1.4 mm head gaskets way better than the 1.8s i had before and the turbo is totally different injectors wernt that bad going up from 800,s to 900,s but looking good .. but been thinking of putting back to std will see how it goes ...chris
#29
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Chris,
What have you used for your fuel pipes? Is it Mocal push on stuff, ala page 239 of the DT motorsport catalogue. JIC to 8mm tails?
Looks good and an interesting alternative to goodridges braided lines and fittings... plus the most appealing thing for me is it's a damm site cheaper!!!!! How you finding it?
Tony.
What have you used for your fuel pipes? Is it Mocal push on stuff, ala page 239 of the DT motorsport catalogue. JIC to 8mm tails?
Looks good and an interesting alternative to goodridges braided lines and fittings... plus the most appealing thing for me is it's a damm site cheaper!!!!! How you finding it?
Tony.