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classic wrx, boost question.

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Old 31 August 2013, 04:06 PM
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scooby kid
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Default classic wrx, boost question.

hi guys,

Hopefully simple boost question, ive recently picked up a early 260hp model Wrx, Runing Arc tmic and the stock td05, fully decatted it make's 1bar then tails off to .9. i presume the 3inch system causes boost creep. Over mods are hks panel filter with full samco turbo inlet and resonator delete and walbro. now as its been so long since owning a scoob or even a turbo car, This one feels feels a fair bit slower than my previous v1 sti that was only dynoed @ 284. The thing iv'e noticed and my main question is on the Lamco gauge ive noticed its taking its time to reach 0.5bar then when hits this it flys down to 1 bar and the car go's well. are they all like this? ive tried removing stock bov and returning no difference, tried dawes device setting it to 1bar no difference.

any advice or is it normal. thinking of going to Surrey R/R to get her fueling checked, with the mods id of thought she would be very close to 290 bhp but really feels like a 220bhp.
Old 31 August 2013, 08:08 PM
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maff125
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actuator or boost solenoid? i had a bit of this and both cured it
Old 31 August 2013, 09:46 PM
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oh right, il try get another actuator as made no difference when used the dawes device. so imagine the solenoid ok thanks..
Old 01 September 2013, 08:47 AM
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I just screwed mine in half a hole, i think the springs weaken with age
Old 01 September 2013, 08:47 AM
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I just screwed mine in half a hole, i think the springs weaken with age
Old 01 September 2013, 12:56 PM
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so removed the of the waste gate, undone the nut and turned it in half a turn?
Old 01 September 2013, 02:29 PM
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i read with interest as iv just bought the same model..95wrx v2...what will this ajustment achieve??
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