Notices
General Technical
Sponsored by:
Sponsored by: CARiD

Boost Levels Dropped?

Thread Tools
 
Search this Thread
 
Old Mar 8, 1999 | 07:12 PM
  #1  
Proby's Avatar
Proby
Thread Starter
Scooby Newbie
 
Joined: Aug 1999
Posts: 17
Likes: 0
Post

Hello folks, I`ve had MY93 WRX for about 3 months now, after having a faulty fuel pump replaced, the car has been fine, until today. The car usually runs at about 0.8 bar when on full bore, but seems to have now dropped to 0.5 bar, leaving the acceleration feel poor. Anybody else had problems, if so, how was it resolved. Cheers, Proby.
Reply
Old Mar 10, 1999 | 09:37 AM
  #3  
Pete Croney's Avatar
Pete Croney
Scooby Regular
 
Joined: Oct 1998
Posts: 4,300
Likes: 0
From: Scoobysport, Basildon, UK
Post

Proby

Are you comparing in like for like situations. Crawling through traffic can cause the engine heat to warm the intercooler and this will result in lower boost pressures. After sufficient cooling from say a motorway drive, the intercooler temperature will fall and boost will be restored.

My car gives an extra 2-4psi on a cold night, compared with a warm day/urban driving conditions.
Reply
Old Mar 10, 1999 | 02:19 PM
  #4  
Fred's Avatar
Fred
Scooby Regular
 
Joined: Oct 1999
Posts: 52
Likes: 0
Post

Hi proby,

what was the symptom when you run before with the defect fuel pump (did the car cut completely the revs during few seconds when you pushed at high boost pressure ? or did you feel little shaked during acceleration?)
Reply
Old Mar 10, 1999 | 09:42 PM
  #5  
Proby's Avatar
Proby
Thread Starter
Scooby Newbie
 
Joined: Aug 1999
Posts: 17
Likes: 0
Post

Hi Folks, thanks for the intrest, the car now seems to be running much better, though sometimes, I seem to get a little flatspot, or a hesitation at 0.5 bar, then it roars up to 0.8 bar. Pete, I did consider climate conditions, but with the, now sometimes `hesitation` I thought maybe ruled that out. Fred, when the fuel pump was on the way out, symptoms were major splutering when coming onto boost, then it got worse and worse, until the car struggled to tick over. Then it would not start at all. I will try cleaning the wastegaste solenoid tommorow with electrical spray cleaner. Cheers guys.
Reply
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
KAS35RSTI
Subaru
27
Nov 4, 2021 07:12 PM
fatboy_coach
General Technical
15
Jun 18, 2016 03:48 PM
psport
Subaru Parts
3
Oct 4, 2015 07:35 PM
Ganz1983
Subaru
5
Oct 2, 2015 09:22 AM
mistermexican
General Technical
2
Oct 1, 2015 04:30 PM




All times are GMT +1. The time now is 01:04 PM.