Notices
ScoobyNet General General Subaru Discussion

Booger - Me Big End Has Gone...

Thread Tools
 
Search this Thread
 
Old Nov 10, 2003 | 03:04 PM
  #1  
Puff The Magic Wagon!'s Avatar
Puff The Magic Wagon!
Thread Starter
Moderator
25 Year Member
iTrader: (2)
 
Joined: May 2000
Posts: 16,980
Likes: 15
From: From far, far away...
Unhappy

There I was, minding my own business & I heard this horrible rattling sound.

So I slowed right down, indicated, pulled off the road & into a garage. Turned the engine off.






The really big bugger about this was that it happened at the begining of my 2nd of 6 sessions @ Brands Hatch

Not a happy bunny


Big thanks to Richard Askew for the tow, Gossy & others for advice, help &noffers of assistance


PTMW! will be back soon



Reply
Old Nov 10, 2003 | 03:17 PM
  #2  
jjones's Avatar
jjones
Scooby Regular
 
Joined: Apr 1999
Posts: 4,410
Likes: 1
Post

unlucky mate

mind you, you got your moneys worth out of that crankshaft

Reply
Old Nov 10, 2003 | 03:23 PM
  #3  
Leslie's Avatar
Leslie
Scooby Regular
 
Joined: Aug 2002
Posts: 39,877
Likes: 0
Post

Sorry to hear about that Puff.

Les
Reply
Old Nov 10, 2003 | 03:33 PM
  #4  
ian_sadler's Avatar
ian_sadler
Scooby Regular
 
Joined: Jan 2001
Posts: 11,170
Likes: 0
From: there or there abouts
Lightbulb

Good job you didn't have a Golf or Ferrari
Reply
Old Nov 10, 2003 | 03:41 PM
  #5  
P20SPD's Avatar
P20SPD
Drag it!
iTrader: (1)
 
Joined: Jun 2002
Posts: 9,866
Likes: 0
From: Flame grilled Wagon anyone?
Post



Sorry James

USDM 2.5 Short Block??
Reply
Old Nov 10, 2003 | 06:28 PM
  #6  
Andy W STI's Avatar
Andy W STI
Scooby Regular
 
Joined: Aug 2003
Posts: 165
Likes: 0
Unhappy

bugger
Reply
Old Nov 10, 2003 | 06:41 PM
  #7  
Leviathan's Avatar
Leviathan
Scooby Regular
 
Joined: Apr 2003
Posts: 746
Likes: 0
Post

Bloody nitemare this! Puff, isnt yours a UK too?
Reply
Old Nov 10, 2003 | 07:11 PM
  #8  
Flat 4x4's Avatar
Flat 4x4
Scooby Regular
 
Joined: Apr 2002
Posts: 1,867
Likes: 0
Thumbs down

Puff

Another UK engine bites the dust. Mine was a 99MY with FSSH and firkin expensive 5W50 Mobil Motorsport - didn't make any difference though.

Can we tempt you yet .... www.briskoda.net
Reply
Old Nov 10, 2003 | 07:13 PM
  #9  
SiDHEaD's Avatar
SiDHEaD
Scooby Regular
 
Joined: Apr 2002
Posts: 9,196
Likes: 0
From: Birmingham
Post

Flat 4x4: it didn't exactly lead a dull life tho

Hope you get it sorted quickly Puff

Andy
Reply
Old Nov 10, 2003 | 07:30 PM
  #10  
CustomScoobyIOM's Avatar
CustomScoobyIOM
Scooby Regular
 
Joined: Jul 2003
Posts: 2,737
Likes: 0
From: Oooooooop North!
Post

Hey Flat4x4 these Skodas are rapid beasties y'know.

Ive got Discos at the moment!
Reply
Old Nov 10, 2003 | 07:31 PM
  #11  
CustomScoobyIOM's Avatar
CustomScoobyIOM
Scooby Regular
 
Joined: Jul 2003
Posts: 2,737
Likes: 0
From: Oooooooop North!
Post

Puff - Sorry mate I know its a pain too. Mines buggered at the moment.

Not for long
Reply
Old Nov 10, 2003 | 07:36 PM
  #12  
Cheesy Puff's Avatar
Cheesy Puff
Scooby Regular
 
Joined: Apr 2003
Posts: 44
Likes: 0
Red face

Sorry to hear that Puff, me and a mate came to watch and were standing up in the big stand for most of the day. I was watching you close as I have a wagon too and I wondered where you had gone, look on the bright side you could have been Magnum P.I. spreading oil and most of your engine around half the track(bet he was popular). What happend to the wheel on that escort? anyway hope you get it fixed soon. It was a great day even as a spectator, maybe Ill have a go next time.

Cheese....
Reply
Old Nov 10, 2003 | 07:40 PM
  #13  
NotoriousREV's Avatar
NotoriousREV
Scooby Regular
 
Joined: Jan 2002
Posts: 11,581
Likes: 0
Post

Sorry to hear that, Puff

Definately time for the 2.5

BTW, you haven't answered my post in the bikers forum
Reply
Old Nov 10, 2003 | 08:02 PM
  #14  
Puff The Magic Wagon!'s Avatar
Puff The Magic Wagon!
Thread Starter
Moderator
25 Year Member
iTrader: (2)
 
Joined: May 2000
Posts: 16,980
Likes: 15
From: From far, far away...
Cool

PTMW! will be back & yes I did console myself that I wasn't the owner of that Ferrari

It wasn't the one, however, that went past me like I was sitting still

2.5 would be nice but as the money for repair will be coming out of my garage fund, I want to be able to have a roof over PTMW! when fixed

However, a select few mods may happen during the rebuild - if nothing else a new clutch (if needed) seeing as the engine will be out - 77k miles on OE with trackdays & 1/4s

Otherwise, we'll see...

Dave - YHM

The Escort has (had) Grp A drive shafts, which are hollow. The NSR sheered straight off They are meant to be be stonger/more reliable but this is the 2nd to go for that owner...


AA took 3 hours to get me on the back of a flatbed

Otherwise, PTMW! was driving well & I'd been just begining to concentrate on getting my lines sorted. For some reason, I hadn't been totally relaxed on the start of the 2nd sesh & they were all over the place I'd been getting a wee bit of u/steer as well, which is unusual. The cage made PTMW! seem well planted and I was very happy with it.

Sorry to POC/Gossy et al who'd wanted pass laps - next time

(& you never know might be a tad faster )
Reply
Old Nov 10, 2003 | 08:12 PM
  #15  
Supercue's Avatar
Supercue
Scooby Regular
iTrader: (1)
 
Joined: Sep 2003
Posts: 6,806
Likes: 0
From: Essex, England
Post

Sorry to see your day cut short James. Glad you got home OK.

At least you didn't have your missus riding shotgun as you spin off on that Ferraris oil slick
Reply
Old Nov 10, 2003 | 08:20 PM
  #16  
-=Buzz=-'s Avatar
-=Buzz=-
Scooby Regular
 
Joined: Mar 2003
Posts: 1,475
Likes: 0
Post

No, no no no no...

DOH! Well, at least it had done a "reasonable" amount of miles

Glad I didn't drive down for a lap!
Reply
Old Nov 10, 2003 | 08:26 PM
  #17  
P20SPD's Avatar
P20SPD
Drag it!
iTrader: (1)
 
Joined: Jun 2002
Posts: 9,866
Likes: 0
From: Flame grilled Wagon anyone?
Post

Puff, mail me. Just gone pas 40000 in mine, coming to a trackday near you soon.
Reply
Old Nov 10, 2003 | 09:36 PM
  #18  
Flat 4x4's Avatar
Flat 4x4
Scooby Regular
 
Joined: Apr 2002
Posts: 1,867
Likes: 0
Post

CustomScoobyIOM

I know...!
Reply
Old Nov 11, 2003 | 09:39 AM
  #19  
TaviaRS's Avatar
TaviaRS
Scooby Regular
 
Joined: Jun 2001
Posts: 9,755
Likes: 0
From: a land full of corsets
Unhappy

Puff, sorry to hear that
Reply
Old Nov 11, 2003 | 09:46 AM
  #20  
Richard Askew's Avatar
Richard Askew
Scooby Regular
 
Joined: Dec 2000
Posts: 9,400
Likes: 0
From: A land of lap-dancers and Lanson Black Label
Post

Invoice for a new clutch on its way I HATE towing

Do you get a tenner for the AA taking so long? If so its a tenner towards the rebuild
Reply
Old Nov 11, 2003 | 12:38 PM
  #21  
mart360's Avatar
mart360
Scooby Regular
 
Joined: Jul 2005
Posts: 12,329
Likes: 0
Question

Super titanium flamesuit on


dare i say it............. hmmmmmmmmm


dunno its definatly controversial ..........


Mart
Reply
Old Nov 11, 2003 | 12:38 PM
  #22  
ALi-B's Avatar
ALi-B
Moderator
20 Year Member
Liked
iTrader: (1)
 
Joined: Apr 2002
Posts: 38,078
Likes: 310
From: The hell where youth and laughter go
Post

Bad news puff

Anyone know what is causing UK turbos to end up like this? I heard all the speculation...just never had anyone to make a statement with a definite fact (that is plausible).

Still, it does me a favour...stops me from spending money on mods in paranoia that said engine will go boom (even if the bottom end has only done 12k )
Reply
Old Nov 11, 2003 | 02:00 PM
  #23  
Puff The Magic Wagon!'s Avatar
Puff The Magic Wagon!
Thread Starter
Moderator
25 Year Member
iTrader: (2)
 
Joined: May 2000
Posts: 16,980
Likes: 15
From: From far, far away...
Post

Whats that then Mart?

The engine had covered 77K miles & 1st reg July 99 with 1 owner/driver. The car has been religeously serviced according to schedule, all bar 2 @ main dealers (60K which included Cambelt & 75K)

The only engine mods were a PPP (zhorst, piping, ecu), so hardly stressed like some other engines with 340+ on standard UK internals. SECS recorded 6900 max RPM (so before limiter) during the sessions & max boost of 1.27 bar. No ECU warnings came up.

It would also be fair to say that I am recognised/known as a smooth and mechanically sympathetic driver, so it would be hard to consider that the big end had gone through abuse and over modification from design specifications and expectations.
Reply
Old Nov 11, 2003 | 03:11 PM
  #24  
EvilBevel's Avatar
EvilBevel
Scooby Regular
 
Joined: Oct 1999
Posts: 3,491
Likes: 0
Unhappy

Weird stuff Puff ...

I was there & saw it happen, you were doing very smooth laps, certainly not stressing or ragging the engine, it was damp/slippery, all went well, then suddenly "rattle of death".

So illogical. So weird.

I'm thinking about a good way to start a new thread about this, calling all people to arms that should know (and they are out there) what is happening with these engines. Let's forget "N°3" (it's not), in fact, we should forget all previous speculation full stop. Oil, high speed cooling probs, fuel pressure, let's throw that away and start from scratch.

It won't help you, but DJ was just pointing out to me that you are indeed a very smooth driver when suddenly you came past the paddock and the car sounded like a bag of nails...

We should finally, after so many years, get to the bottom of this.

Theo

PS: nice seeing you in the flesh, you are as ugly as I imagined, but I guess that goes both ways
Reply
Old Nov 11, 2003 | 03:14 PM
  #25  
Richard Askew's Avatar
Richard Askew
Scooby Regular
 
Joined: Dec 2000
Posts: 9,400
Likes: 0
From: A land of lap-dancers and Lanson Black Label
Post

Theo - you home already?
Reply
Old Nov 11, 2003 | 03:17 PM
  #26  
David_Wallis's Avatar
David_Wallis
Scooby Regular
 
Joined: Nov 2001
Posts: 15,239
Likes: 1
From: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
Post

Theo good idea.. 22b or here?

David
Reply
Old Nov 11, 2003 | 03:42 PM
  #27  
EvilBevel's Avatar
EvilBevel
Scooby Regular
 
Joined: Oct 1999
Posts: 3,491
Likes: 0
Post

Rich, yeah, cuz you woke us up this morning [img]images/smilies/mad.gif[/img]

David, no preference, let me have a think (uh oh ... )
Reply
Old Nov 11, 2003 | 03:46 PM
  #28  
Richard Askew's Avatar
Richard Askew
Scooby Regular
 
Joined: Dec 2000
Posts: 9,400
Likes: 0
From: A land of lap-dancers and Lanson Black Label
Post

Sorry - I did *try* to leave quietly Was awake most of the night cos of Shauns ability to belch/fart/snore non stop for 6 hours
Reply
Old Nov 11, 2003 | 03:58 PM
  #29  
john banks's Avatar
john banks
Scooby Regular
 
Joined: Nov 2000
Posts: 18,658
Likes: 1
From: 32 cylinders and many cats
Post

SECS would show 1.27 bar even if the real boost is far higher - it clips at 1.27 bar and this is overboost really for a PPP. With the ignition timing used on the PPP map this could easily cause detonation. This means you were at least 0.19 bar over PPP's boost target. On a hot track when the EGTs get high the turbo can get very frisky and cause overboost. When running boost controllers at over 1.2 bar with (decat) PPP at Knockhill on plain Optimax, it started detting. The decat may help or hinder the det through various mechanisms.

Det avoidance is the one big reason the big power tuned engines tend to stay together. However, I am not saying the only cause of failure is detonation by no means.

[Edited by john banks - 11/11/2003 4:02:48 PM]
Reply
Old Nov 11, 2003 | 04:02 PM
  #30  
ALi-B's Avatar
ALi-B
Moderator
20 Year Member
Liked
iTrader: (1)
 
Joined: Apr 2002
Posts: 38,078
Likes: 310
From: The hell where youth and laughter go
Thumbs up

Good Idea Theo.

Personally, my 2p is it's either: poor bearing material quality, Oil surge, pressure leakage, or some sort of flow problem.

[Edited by ALi-B - 11/11/2003 4:03:21 PM]
Reply



All times are GMT +1. The time now is 11:16 PM.