Can I have your opinion on these symptoms pleeaasseee
#31
Orange Club
iTrader: (11)
DV isn't in front of the airbox is it, which is where the OP said this is? I wondered if it might have been the fuel pressure regulator, but lack of clips on the thicker pipes rules that out I think.
But, I agree that the thinner pipe looks vacuum related...so maybe related to boost control solenoid?
Either way, it being trapped cannot be right, so I would remove airbox, free and/or replace the pipe and test again.
But, I agree that the thinner pipe looks vacuum related...so maybe related to boost control solenoid?
Either way, it being trapped cannot be right, so I would remove airbox, free and/or replace the pipe and test again.
#32
Scooby Regular
iTrader: (13)
No, I'm 99% certain that's a black plastic "in-line" MY93-96 recirc DV (looking at it from the underside)!
But if it has been fitted to a MY00, then it will have been modded to make it fit, as the MY00 TMIC has a cast flange for the OEM metal DV (assuming the OEM MY00 TMIC is still present). So it's position will not necessarily be where you'd expect it, comapred to a MY93-96 car, IYSWIM.
Simonds, can you post some pics up of the whole of your engine bay? - we need to get to the bottom of this aspect....
But if it has been fitted to a MY00, then it will have been modded to make it fit, as the MY00 TMIC has a cast flange for the OEM metal DV (assuming the OEM MY00 TMIC is still present). So it's position will not necessarily be where you'd expect it, comapred to a MY93-96 car, IYSWIM.
Simonds, can you post some pics up of the whole of your engine bay? - we need to get to the bottom of this aspect....
Last edited by joz8968; 25 April 2010 at 11:24 AM.
#38
Scooby Regular
iTrader: (13)
If it isn't the early DV (and it's obviously odds on that it isn't, as Micky points out), then my sincerest apologies OP. Forget my ramblings, etc.
But if you could take a pic of the item a bit futher out, so we can see the other stuff around it and more of the engine bay etc, that would get our heads around (mine at least) what we're looking at, etc....
But if you could take a pic of the item a bit futher out, so we can see the other stuff around it and more of the engine bay etc, that would get our heads around (mine at least) what we're looking at, etc....
Last edited by joz8968; 25 April 2010 at 11:34 AM.
#39
Scooby Regular
Thread Starter
Join Date: Nov 2006
Location: Pembrokeshire, South Wales
Posts: 639
Likes: 0
Received 1 Like
on
1 Post
It's the thing I've circled green in the close up view. Dunno what it is, but one pipe from it seems to go to a little cylindrical thing at the front? Carbon canister sorta thing is it? Then another pipe comes off it and goes to the main big air intake coming off the airbox, and then another seems to go back to all the boost pipework around the turbo/boost solenoid etc
#40
Scooby Regular
iTrader: (13)
Yeah, tim was right, it's some kinda valve to do with the oil breathing system (if it is a valve, then ironically it would work just like a recirc DV - but, presumably, diverting oil fumes/vapours instead! ). But sorry tim (and micky ).
But if it defo has a vac pipe relating to the the BCS system, and is crushed/collapsed/split in anyway, then defo replace it with a fresh new one!
It may not be the reason for your problems in itself... but it certainly ain't gonna help your situation. So yeah, replace it FIRST, then go out for another drive, etc. and report back...
But if it defo has a vac pipe relating to the the BCS system, and is crushed/collapsed/split in anyway, then defo replace it with a fresh new one!
It may not be the reason for your problems in itself... but it certainly ain't gonna help your situation. So yeah, replace it FIRST, then go out for another drive, etc. and report back...
Last edited by joz8968; 25 April 2010 at 12:51 PM.
#41
Simonds, have had the weekend off so not had a chance to look at your post in full yet - will have a proper squizz tomorrow. However, just to give the ball a bit of a kick...
Joz, that isn't the DV it's the canister purge valve. Orientation of the pic is a little confusing, but it's offside flitch panel we're looking down at. The airbox you can see in the upper left, timing belt cover in the lower right, and the MAF tube running across top of frame.
Simonds, that pipe shouldn't really be tight, sounds like it's trapped under the airbox and that's stretching it a little. All that stuff, the carbon canister included, is for vapour control/emissions compliance. No harm in you pulling the tube off and giving it a good visual inspection for splits. Air getting in anywhere it's not supposed to can cause all sorts of weird stuff. Speaking of which, make sure the elbow on the end of the canister purge pipe is stuck in its hole in the air link pipe (the big one that goes from the MAF tube to the engine). Looks like it is in your photo, but better to check it.
As regards the O2 sensor, it's not at all surprising to hear you haven't got the CEL despite leaving it disconnected, so no this is nothing to worry about. As you can see from your log, the O2 sensor signal line floats at around 0.34 volts when left open circuit. If I remember right it has to be either 0.00 volts for a certain period of time, or over 1.2 volts, again for a period of time, before the error state is set.
Anyway, I'm orf, more tomorrow/
Joz, that isn't the DV it's the canister purge valve. Orientation of the pic is a little confusing, but it's offside flitch panel we're looking down at. The airbox you can see in the upper left, timing belt cover in the lower right, and the MAF tube running across top of frame.
Simonds, that pipe shouldn't really be tight, sounds like it's trapped under the airbox and that's stretching it a little. All that stuff, the carbon canister included, is for vapour control/emissions compliance. No harm in you pulling the tube off and giving it a good visual inspection for splits. Air getting in anywhere it's not supposed to can cause all sorts of weird stuff. Speaking of which, make sure the elbow on the end of the canister purge pipe is stuck in its hole in the air link pipe (the big one that goes from the MAF tube to the engine). Looks like it is in your photo, but better to check it.
As regards the O2 sensor, it's not at all surprising to hear you haven't got the CEL despite leaving it disconnected, so no this is nothing to worry about. As you can see from your log, the O2 sensor signal line floats at around 0.34 volts when left open circuit. If I remember right it has to be either 0.00 volts for a certain period of time, or over 1.2 volts, again for a period of time, before the error state is set.
Anyway, I'm orf, more tomorrow/
#43
Scooby Regular
Thread Starter
Join Date: Nov 2006
Location: Pembrokeshire, South Wales
Posts: 639
Likes: 0
Received 1 Like
on
1 Post
I haven't had a chance to go out for another drive yet and do an ECU explorer log with my lambda sensor back on. It's back on now by the way, I re-connected it on saturday. Car doesn't seem any different at all. I also still haven't heard back from Bob yet. Thanks Splitpin, appreciate your message even tho you've had the weekend off. Look forward to hearing more from you!
#45
From the logs to me it looks quite clear:
The turbo is only boosting to the actuator pressure of about 7-8psi when you are seeing issues. Therefore a likely cause is that the boost control solenoid wires are a bit suspect and the valve is sometimes not bleeding the air required to increase the boost pressure past the 7 psi that the actuator. That or there is something moving and blocking the pipe where it bleeds.
It may be worth checking that the wires around the ECU haven't been chopped and stuck back together if someone had an aftermarket boost controller installed one time.
It certainly looks to be a boost control issue - if you had a boost gauge you'd probably be able to see it stick at about 0.5bar when its not working correctly.
The turbo is only boosting to the actuator pressure of about 7-8psi when you are seeing issues. Therefore a likely cause is that the boost control solenoid wires are a bit suspect and the valve is sometimes not bleeding the air required to increase the boost pressure past the 7 psi that the actuator. That or there is something moving and blocking the pipe where it bleeds.
It may be worth checking that the wires around the ECU haven't been chopped and stuck back together if someone had an aftermarket boost controller installed one time.
It certainly looks to be a boost control issue - if you had a boost gauge you'd probably be able to see it stick at about 0.5bar when its not working correctly.
#46
Well that's good to know. I still don't know why the 2nd log from my previous post only shows a throttle sensor voltage of 3.76v when I thought I had my foot flat down. I can't be 100% sure to be honest, so I think the actual reason is more than likely my foot was not fully down.
If you can get some more log data, especially when the car's acting up, it'd help rule this explanation in/out.
every morning when I go to work the car seems to be in a different 'mood' as far as idling/revving is concerned. Some mornings it just wants to rev. This is only when I'm pottering along, not doing much over 1,700rpm sorta thing, and when the engine is cold. Never really thought anything of this before, but thought it might be worth mentioning now.
From the logs to me it looks quite clear:
The turbo is only boosting to the actuator pressure of about 7-8psi when you are seeing issues. Therefore a likely cause is that the boost control solenoid wires are a bit suspect and the valve is sometimes not bleeding the air required to increase the boost pressure past the 7 psi that the actuator. That or there is something moving and blocking the pipe where it bleeds.
The turbo is only boosting to the actuator pressure of about 7-8psi when you are seeing issues. Therefore a likely cause is that the boost control solenoid wires are a bit suspect and the valve is sometimes not bleeding the air required to increase the boost pressure past the 7 psi that the actuator. That or there is something moving and blocking the pipe where it bleeds.
The ECU actively monitors the connection to the solenoid and an open (or short) circuit longer than 0.4 of a second is enough to trigger the CEL with code 44. That log extract Simonds posted shows a WOT sequence of over 5 seconds during which the turbo is notably failing to boost - yet as far as we know there's no CEL. This tends to suggest there's nothing major at fault with the connection to the solenoid, although agree totally it's something to look at.
In addition, as you say the maximum pressure recorded on the log is around where the actuator crack would be. However, it's in the higher end of that range and the behaviour of the turbo in the log is not consistent with what you'd expect in this scenario. There you would expect the turbo to spool normally, hitting actuator pressure at around 2400-2600 rpm and then continuing to hold pretty much the same MRP until the throttle is released.
In the first log excerpt, the engine is already at 2800rpm at the moment full throttle is applied, having got there on part throttle (so the turbo should be reasonably well spooled already). Yet, it still takes another four seconds to hit peak pressure. That's not what you'd expect in a scenario where everything was otherwise working fine, but the actuator was either effectively disconnected from its power supply, or the bleed outlet blocked somehow.
In addition, your theory doesn't easily explain the two rows of data at 13:30.3 and 13:30.7. Despite, as above, taking four seconds to get to a measly 8.7psi, in those two rows we are expected to believe that the manifold relative pressure more than doubled in 0.4 of a second, despite the log indicating that the throttle has been shut - corroborated by the drop in mass airflow voltage indicating a reduction in intake to idle levels (albeit that the boost duty remains at 81% for that. That bit's really weird, although may be explained by the custom map.
It may be worth checking that the wires around the ECU haven't been chopped and stuck back together if someone had an aftermarket boost controller installed one time.
It certainly looks to be a boost control issue - if you had a boost gauge you'd probably be able to see it stick at about 0.5bar when its not working correctly.
Simonds1, some more logs, with the O2 sensor connected, both of a normal/good acceleration run from around 2200rpm up to mid 4500's (genuine WOT ) for comparison, and another genuine WOT run when it's acting up, would be very handy.
Also (and apologies for the brain fade if we've done this before), do you have a standard or aftermarket dumpvalve, and when Bob mapped it, did you ask him to add some overt "pops and bangs" on lift-off?
Last edited by Splitpin; 27 April 2010 at 04:07 PM.
#47
Splitpin I agree with everything above but will point out that the logs that I've taken before can be a little misleading. I have often seen spurious zeros or meaningless data and also noticed that some values appear to be correct but for the iteration before (or after). Basically the update rate isn't all that fast and it its also possible the CPU is actually quite busy and doesn't update the values that are acquired over OBD that often either (or at least not all at the same time) therefore its possible to get some updated data and some delayed.
Also of note: if you do not have a valve bleeding air out of the waste gate actuator pipe then the wastegate will start to open before the 7psi set point and slow the spool - but I agree it should probably be much faster than it was.
The same principle applies to closed loop boost control where the controller will go to near 100% duty cycle right up until the last point it can before reducing it to prevent overshoot. This means the wastegate it shut for the entire spool. Therefore if you don't have it bleeding any air at all (pipe blocked, wires dodgy) it will slow the spool.
Comparing the two logs at about 2800 rpm however shows something interesting - the first has a small amount of boost but that would only push it to a richer part of the map, but actually has a lower injector duty than the second log. This could again be down to issue with the update speed of the data being returned (esp as result 2 was second gear and values change fast)
The best thing it to try and get result in 4th gear - you'll get lots more (hopefully meaningful) data. Bit harder to find good road conditions though...
Also of note: if you do not have a valve bleeding air out of the waste gate actuator pipe then the wastegate will start to open before the 7psi set point and slow the spool - but I agree it should probably be much faster than it was.
The same principle applies to closed loop boost control where the controller will go to near 100% duty cycle right up until the last point it can before reducing it to prevent overshoot. This means the wastegate it shut for the entire spool. Therefore if you don't have it bleeding any air at all (pipe blocked, wires dodgy) it will slow the spool.
Comparing the two logs at about 2800 rpm however shows something interesting - the first has a small amount of boost but that would only push it to a richer part of the map, but actually has a lower injector duty than the second log. This could again be down to issue with the update speed of the data being returned (esp as result 2 was second gear and values change fast)
The best thing it to try and get result in 4th gear - you'll get lots more (hopefully meaningful) data. Bit harder to find good road conditions though...
#48
(or at least not all at the same time) therefore its possible to get some updated data and some delayed.
As I've said previously it is possible to miss transient changes in value "between" samples (especially on that 0.4 second refresh rate), but having a row of a datalog which contains a mix of current values and "delayed" ones is not possible on a JECS.
If there are errors in Simond's log data, the only point at which they could creep in is if ECU Explorer is introducing them, although given how simple the software is - it gets one packet of data, displays (and logs it) and goes back to get another, it's difficult to see how a delay of this kind can creep in at the PC end. About the only explanation for duff figures would be if the software is very intolerant to communication errors of the sort caused by electrical interference in the diagnostic signal line, the USB-serial port not being tied properly to the JECS ECUs non-standard serial timing or so-on. Under those circumstances though you'd expect it to display obviously garbled info rather than errors too subtle to immediately notice, Even then you'd expect the software to disregard any packet with a checksum error.
As you say, more log data would be very illustrative here.
Last edited by Splitpin; 27 April 2010 at 06:07 PM.
#49
Scooby Regular
Thread Starter
Join Date: Nov 2006
Location: Pembrokeshire, South Wales
Posts: 639
Likes: 0
Received 1 Like
on
1 Post
Here's a link to the log file, same mailbigfile thing as before so will only be available to download for 5 days or so.....
http://mbf.me/6hgt
The refresh time was hovering around 196ms, and also I had chosen the "convert injector pulse width to duty%" option because I'm sure someone mentioned that before? I'm sorry if that causes problems with comparing & contrasting to my first logs, as I didn't have that option on then.
So here's a rough explanation of what was happening and when......
39:44.1 - Really really brief uphill 2nd gear full throttle accelerate. Car went well and seemed pretty normal.
42:25.6 - Uphill full throttle accelerate in 3rd. Car went well and seemed pretty normal again.
45:22.6 - Level ground, really really brief full throttle accelerate in 4th. Car seemed to start picking up good and normal but then I had to let off.
47:44.7 - Uphill full throttle accelerate in 2nd gear and the car was RUBBISH! Barely moved, not boosting, caught in the act thank god! Was thinking it wasn't gonna faulter on this journey cuz it'd seemed good up until now.
51:42.6 - Just incase any of you notice my revs seeming a bit odd around this time, it was me trying a full throttle accelerate on a flat bit of road in 4th, and my clutch slipped lol.
52:02.4 - Level ground, full throttle accelerate in 3rd, and the car seemed okay to me. It definitely didn't do it's 'fault', but it also didn't seem to go as well as it could've done. I dunno, it's so hard to tell whether the car is actually slower than it's meant to be or not, because I might just be getting used to the power, or it might actually have faultered in some way. I don't know! Just generally doesn't seem as quick as it should be, even when it 'succesfully' accelerates now. But maybe that is just down to me being used to the power.
57:27.7 - Level ground, 3rd gear full throttle, then into 4th full throttle accelerate. Car seemed good and went well.
58:13.2 - Level ground, quite brief 3rd gear full throttle accelerate. Car went well and seemed normal.
58:50.7 - Level ground, quite brief 4th gear full throttle accelerate (no clutch slip this time!). Car seemed good and went well.
00:30.9 - Uphill, full throttle accelerate in 3rd gear. Car seemed good and went well.
That's all of the 'important' parts I noted down to mention. Everything else is just boring driving around in between the accelerating bits. So it only really faultered once on the whole journey, whereas the last log I did - same journey & same accelerating points, it faultered 3 times! I hate intermittent faults!!! Grr! Oh, by the way... even though the times I've noted down there are very specific, they are only to give you a rough idea of where to look in the log if y'know what I mean? But yeah I'm sure you can work that out by looking at them. I hope they help anyway.
On the subject of boost pipework, do you think it's a good idea for me to buy some samco vaccuum tubing and replace all my vaccuum hoses just incase one of them is at fault? Or do you think that's overkill?
Couldn't agree more! I'm still quite amazed at how willing people that I don't even know are willing to help me with this problem! It really is awesome, and like dnc said, it's what these forums are all about. So yeah, massive thanks again everyone. I think that's everything for now? I look forward to your responses!
#50
Scooby Regular
Thread Starter
Join Date: Nov 2006
Location: Pembrokeshire, South Wales
Posts: 639
Likes: 0
Received 1 Like
on
1 Post
The ECU actively monitors the connection to the solenoid and an open (or short) circuit longer than 0.4 of a second is enough to trigger the CEL with code 44. That log extract Simonds posted shows a WOT sequence of over 5 seconds during which the turbo is notably failing to boost - yet as far as we know there's no CEL. This tends to suggest there's nothing major at fault with the connection to the solenoid, although agree totally it's something to look at
#51
Off topic but it IS possible to have some non-updated data if the UART buffer is small. The reason is that the UART will be on a very low interrupt priority, and other tasks won't be and can take priority. You will notice if you do a lot of logging that the log update rate reduces as the engine speed/load increases. Why would that happen if the MCU wasn't busy doing other things (like detecting more and more crank and cam sensor zero crossings).
It does however from that log still (to me) look like the boost control solenoid is not working at the points at which you have issues and you are just seeing actuator boost. I would definitely check the wires that run to the solenoid, as well as check that the two pipes either side of the solenoid run free without being pinched by anything if the engine is rocking.
It does however from that log still (to me) look like the boost control solenoid is not working at the points at which you have issues and you are just seeing actuator boost. I would definitely check the wires that run to the solenoid, as well as check that the two pipes either side of the solenoid run free without being pinched by anything if the engine is rocking.
#52
You will notice if you do a lot of logging that the log update rate reduces as the engine speed/load increases.
Why would that happen if the MCU wasn't busy doing other things (like detecting more and more crank and cam sensor zero crossings).
#53
Scooby Regular
Thread Starter
Join Date: Nov 2006
Location: Pembrokeshire, South Wales
Posts: 639
Likes: 0
Received 1 Like
on
1 Post
No worries, thankyou for helping me with all this! I still haven't heard back from Bob I was hoping he'd email me back like "yeah, I know exactly what's wrong!", but I'm starting to think this is gonna be a pretty un-solveable problem without a lot of trial & error of me replacing things. At least we can narrow down the things for me to try replacing I spoze. Ah well, see if anyone comes up with anything!
#54
Scooby Regular
Thread Starter
Join Date: Nov 2006
Location: Pembrokeshire, South Wales
Posts: 639
Likes: 0
Received 1 Like
on
1 Post
Hey guys, just trying to keep this going. I've just been out and done another log () and I think I've noticed a pattern. I've just been back over all my previous logs to check, and the pattern is pretty much true in all of those aswell. In the sections of the logs when the car is suffering from the non-accelerating problem, the ignition timing is always about double what it is in the sections when the car is accelerating successfully. Forgive me if I'm pointing out something blindingly obvious or irrelevant here, as I really don't understand enough about what I'm actually looking at.......but does that mean anything to anyone? Seems odd to me?
#58
Hey guys, just trying to keep this going. I've just been out and done another log () and I think I've noticed a pattern. I've just been back over all my previous logs to check, and the pattern is pretty much true in all of those aswell. In the sections of the logs when the car is suffering from the non-accelerating problem, the ignition timing is always about double what it is in the sections when the car is accelerating successfully. Forgive me if I'm pointing out something blindingly obvious or irrelevant here, as I really don't understand enough about what I'm actually looking at.......but does that mean anything to anyone? Seems odd to me?
From the first 2 logs you posted (not ideal as has been mentioned because you needed to be in 3rd or 4th gear for both from a similar start speed then WOT) it appears to me that your problem is a lack of boost pressure.
Before investigating this in more detail you should flush through your two-port boost solenoid with petrol or carb/brake cleaner to see if things improve. If not then you can move on to check the cracking pressure on the wastegate actuator and of course remove the small lengths of boost piping between turbo nipple and wastegate (t-piece in middle and also the brass restrictor pill in the turbo to t-piece section) to check for damage and that the pipework is clean inside (can get oil contaminated).
Don't buy any of that crap Samco 3mm vacuum tubing because it is just silicon tube and therefore doesn't retain its shape under pressure or vacuum.
Kevin
#59
Scooby Regular
Thread Starter
Join Date: Nov 2006
Location: Pembrokeshire, South Wales
Posts: 639
Likes: 0
Received 1 Like
on
1 Post
I suppose a good start point would be to find out which one is actually the boost solenoid (A, B, or C below), and which pipes I have to spray in or take off etc?.......
Thanks very much in advance guys! Appologies that I am so stupid