hesitation, classic between2-3k need help
please help, have a 99 uk turbo classic, totally standard, it has a problem where there is quite a hesistation between 2-3k and when driving along say in 5th at 60 when the revs are there it feels like the power is pulsating, coming and going.......have replaced ignition leads and i am thinking either coil pack or fuel pump, have changed maf but never made any difference??
anybody come across this problem before, car runs fine otherwise and seems to boost and pull fine there is no fault codes and engine management light has never came on..... thanks in advance... |
Have you looked at the sparkplugs ?
Mine done that, when I had a bad gap setting on them. |
Originally Posted by slipstream_uk
(Post 9162329)
Have you looked at the sparkplugs ?
Mine done that, when I had a bad gap setting on them. |
bttt please help needing the car next week for g/f, someone must have a idea or two.......
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Maybe your boost solenoid. Give it a clean.
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Is it , mapped etc..? Need to know more..! ;)
If it's previously melted a piston it sounds like it might be detting, although at <3k that's a bit unlkely imho..?? Hence the need to know more info about spec..;) |
Any modifications? what fuel are you running? (all the usual questions as if you didnt fix why it melted a piston then it will probably do it again :( )
Tony:) |
Mine's doing this. I found a loose boost hose clip which I tightened and it's improved matters. Worth checking :)
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hi thanks for the ideas, just to add some info, the car is a standard uk turbo only mod is a back box, still has all cats.......run car on both unleaded and super still has problem with both........will check boost pipe but never noticed anything when it was stripped..have given the boost control a clean but problem seems to be before the boost comes in once in car goes fine...
tony i know getting worried as this is the "reliable" family car so can't really risk it doing it again, plus am i right in saying its rare for no2 piston to melt... thanks for info and help so far |
Originally Posted by SiofChester
(Post 9163745)
Mine's doing this. I found a loose boost hose clip which I tightened and it's improved matters. Worth checking :)
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Originally Posted by scoobywag
(Post 9163870)
will remove intercooler incase the plastic pipe underneath has split??? did yours boost and go ok above 3k??
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May be worth putting a can of injector cleaner through it? I had a mysterious hesiation and it cleared it up...
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will try the injector cleaner, then replace intercooler at weekend hopefully, any other ideas welcome
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20 quid says o2sensor , or o2sensor white plug to the left of the intercooler coroded inside !
and get the faultcode out of the car. |
Yup its very rare for no2 to go, especially on a standard car, normally points to bad fuelling though, could be your fuel pump is a little weak :( or its one of the sensors (maf springs to mind as they are quite fragile on MY99/00 cars).
Tony:) |
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