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MY. 02 WRX ..... the story so far

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Old Dec 30, 2004 | 12:57 PM
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Default MY. 02 WRX ..... the story so far

Spec .

2002WRX
Motec M800 pro
USDM 2.5 sti block
wrx cams
polished heads
cp pistons block machined to fit new pistons
ballanced crank
900cc injectors
Trust FMIC
custom fuel rails (made by me)
custom equal length headers (me)
custom up pipe(me)
Tail 40mm ext waste gate
hybrid T61 turbo
fuel lines all changed to 9mm aero quip push on
2xwalbro 255,s in tank
erl water inj

there is mor i will remember later


drive train

cusco twin plate clutch
sti2 ger box fitted with PPG 3/4
quick shift
plated rear diff
open front diff
std drive shafts
std prop
tein coil overs
brembo gran turismo 330mm brake kit

wheels

Compomotive MO 8/18
yoko AVS sport 225/40/18

Exterior
C/F bonnet soon to go want std wr blue one back anyone.
C/F S202 rear spoiler swap for hi sti7/8 in wr blue

Interior
car came std with UK300 interior ble alcatera
PLX wide band
gredy boost guage
greddy egt
greddy oil press
sony head unit









well after 5k+ mils and 4 gear boxes it gave up the ghost and broke the ring lands
on 3 pistons on comp test No 2 was down to 75psi . but considering that this was done not as bad but quite bad when it went on rollers at well lane and did
421bhp not bad i supose .. well i finnished off the engine yesterday and up and running at 11pm last night .

i built the new engine with new pistons,bearings,turbo,
used Cometic 1.4mm head gaskets and std Subaru bearings
and CP pistons with new Subaru rings i have lots of other bitts to go on in time .

will up date as i go on ..... chris

Last edited by wrrjones; Dec 30, 2004 at 01:00 PM.
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Old Dec 30, 2004 | 04:10 PM
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How come you want to get rid of the bonnet Chris?
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Old Dec 30, 2004 | 05:11 PM
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Great manifolds!
911
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Old Dec 30, 2004 | 05:31 PM
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Originally Posted by AlanG
How come you want to get rid of the bonnet Chris?

just want a change want to get the car looking more std again.... chris
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Old Dec 30, 2004 | 07:13 PM
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Cheers Chris.
Curious.. did you leave the ext. wastegate vent open to atmosphere?

P.S. more pics please!!

Last edited by AlanG; Dec 30, 2004 at 07:15 PM. Reason: addition
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Old Dec 30, 2004 | 07:45 PM
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yes it vents under the car ..lol... ill get mor pics tomorrow as ive got re site the fuel filters .......
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Old Dec 30, 2004 | 10:19 PM
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Were you running the 2.5 Litre block as standard internals then I take it?

Jon.
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Old Dec 30, 2004 | 10:31 PM
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From: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
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look like obx headers..

It was a std block with a slight overbore iirc.
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Old Dec 31, 2004 | 10:10 AM
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slight hone not over bore but still shgged the ring lands ....... not std anymore....chris
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Old Dec 31, 2004 | 01:59 PM
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What did you think of the Trust FMIC?

Jon.
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Old Dec 31, 2004 | 03:51 PM
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From: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
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Did you crack a ring land? what damage to the piston?

How do you think you damaged the ring lands??

David
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Old Dec 31, 2004 | 05:53 PM
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David

ill post up pics of pistons 3 pistons with ringland failure 1 is realy bad other 2 are just bad
failure was down to too much boost i.e 2bar before 1.5 was fine when i removed the pistons the ringlands on 1 piston just fell out looked like they had been plasma cut lol...chris

Jon.

i like the FMIC seems to work well i have a new one in case .....chris
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Old Jan 2, 2005 | 06:52 PM
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Default more pics







pics of 2 of the damaged pistons the cracked sections actually dropped out when i removed rings.





just have a couple of jobs left to do like re site the fuel filters still need a 2.5ins 45deg samco that should be here on tues lets see need some more exhaust wrap lol...



chris

Last edited by wrrjones; Jan 2, 2005 at 06:54 PM.
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Old Jan 2, 2005 | 09:34 PM
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Old Jan 2, 2005 | 11:59 PM
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I don't know about cracking the ring lands, more like shattering them!!
Looks like you took a chisel to them

Dan.

P.S. Thanks for the peek under the bonnet in the que at the Pod, some good time u run that day too!
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Old Jan 3, 2005 | 09:30 AM
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How come you've got two cables going to the throttle body linkage Chris?
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Old Jan 3, 2005 | 12:13 PM
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One for anti lag.

Cant believe you went for the Red inlet after all esp after what that kid said at the pod

Rob

Last edited by tweenierob; Jan 3, 2005 at 12:15 PM.
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Old Jan 3, 2005 | 05:12 PM
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i forgot all about that hmmmm colour change coming me thinks .....

the second cable kicker for anti lag as Rob says .... chris
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Old Jan 4, 2005 | 03:40 PM
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{Interested} How does that work?
PM, if you don't want to fill up your project thread with my drivel. lol
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Old Jan 5, 2005 | 05:06 PM
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Originally Posted by AlanG
{Interested} How does that work?
PM, if you don't want to fill up your project thread with my drivel. lol

Alan

it acts like a hand throttle keeping the butterfly open at i.e 2500 rpm so on gear change the buttefly never shuts ie feeding the antilag ..... you want some more pics ???... chris
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Old Jan 5, 2005 | 07:51 PM
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Originally Posted by wrrjones
David

ill post up pics of pistons 3 pistons with ringland failure 1 is realy bad other 2 are just bad
failure was down to too much boost i.e 2bar before 1.5 was fine when i removed the pistons the ringlands on 1 piston just fell out looked like they had been plasma cut lol...chris

Jon.

i like the FMIC seems to work well i have a new one in case .....chris
2bar of boost on the stock rods ?????

Carlos
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Old Jan 5, 2005 | 10:19 PM
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how long were you running 2 bar for?

I've had a few 2 bar spikes!!
I wasn't planning on running that high
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Old Jan 6, 2005 | 08:28 AM
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Carlos..

the rods arnt the problem and in inspection they were mint no probs at all the pistons wont take any more than 1.5 reliably and any one that exeeds that is looking for trouble ... was running 2.2 bar at one point when the pistons were poorly to see how everything stood up and every thing else was fine ran 2+ bar for 1000 mils maby more but the engine was breathing heavly by this time and i wanted to see how it went as i had spare short motor which was rebuilt with forged internals by me to slot in ...

Dyney

are you on 2.5 usdm sti?..
if so i would be realy carefull with std pistons and make sure you keep the boost down
if not take a look at my pistons ..... chris
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Old Jan 6, 2005 | 03:23 PM
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it acts like a hand throttle keeping the butterfly open at i.e 2500 rpm
Interesting.. didn't know you could do it this way.

More pics if you have them?
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Old Jan 6, 2005 | 04:34 PM
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From: Leeds - It was 562.4bhp@28psi on Optimax, How much closer to 600 with race fuel and a bigger turbo?
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carlos has some good pics of his on 22b a while ago...

Motec also sell a throttle kicker for this.

David
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Old Jan 6, 2005 | 08:10 PM
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yeah they do but i all ready had this one made by Apexi works well enoughand its realy sensitive so easy to make minor adjustments and 1 click off dont have to wind it back in ill get some more pics tomorrow of the set up inside the car as i will be out with the laptop lol as its been out for first run today the set up is tptally different to last one getting det at 0.5 bar lol.... ... chris

Last edited by wrrjones; Jan 6, 2005 at 08:13 PM.
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Old Jan 7, 2005 | 09:26 PM
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4k miles and counting
Only running 1 bar though.

Thanks for the warning
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Old Jan 13, 2005 | 10:07 AM
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well been mapping and up to 1.5 bar atm and all going well cant beleve everything is so different on new eng from last build and mapping ,, ie pistons rods 1.4 mm head gaskets way better than the 1.8s i had before and the turbo is totally different injectors wernt that bad going up from 800,s to 900,s but looking good .. but been thinking of putting back to std will see how it goes ...chris
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Old Jan 13, 2005 | 03:53 PM
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Chris,

What have you used for your fuel pipes? Is it Mocal push on stuff, ala page 239 of the DT motorsport catalogue. JIC to 8mm tails?

Looks good and an interesting alternative to goodridges braided lines and fittings... plus the most appealing thing for me is it's a damm site cheaper!!!!! How you finding it?

Tony.
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Old Jan 13, 2005 | 04:39 PM
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Think its the same stuff as that Tony, having seen it on chris's car. Its also what pavlo uses from memory. Its even cheaper from Think Automotive.
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