Decisions
My 07 hawk wrx got remapped last year with a vf48 turbo and supporting mods and on the way home from the tuner the car started putting thick grey smoke out of the exhaust, and there is the same smoke coming out of the breather pipes and the oil filler neck. The catch cans filled with oil almost instantly.
im assuming its piston failure, possible even more. The car has a whole list of mods and was my baby until this happened at the start of the year and has since been locked away in the garage. now decisions. Do i a. Rebuild it? Not sure how much i should expect to spend to have a nice weekend car nothing to crazy b. Admit defeat and sell up? Ive just bought a house so could really do with the extra money. Is a hawk wrx needing a rebuild still worth anything? any info or advice would be appreciated cheers |
Sell up.
A money pit that time has passed by. I wish I'd sold mine when I had chance. Worth more if I break it now and can't be arsed with that game. |
Would blown turbo oil seals give the same symptoms?
Was the engine knocking? |
No theres no engine knock. The car had remap, turbo fitted, new walbro 255, 3" decat, and got 2 catch cans fitted. The air pump was removed to. It didnt feel that much difference considering it should have been 50hp more. Must have drove no more than 50miles ish and it started to loose power as if it was on 3 cylinders and there was thick grey smoke behind me
|
What turbo was in it? Td04?we're the vf48 coolant&oil lines/banjo bolt used?
also was the pcv still used with the catch cans? |
It was a vf48 that i had fitted. I took it to a reputable place with all the bits and had them fit them for me. I supplied the banjo bolts so assuming they fitted them.
i rang them when i pulled over half way home from remap and explained what had happened and they said it was probably piston failure. I wouldnt of minded if i was kicking its head in but i was doing 50mph in 5th |
Not sure if pcv still used. He said he removed airpump and fitted 2 catch cans. Im sure its 1 for the crankcase and the other for something else
|
Could well be piston failure,have you dropped the rest of the oil and checked for bits of metal?
|
No i was that pissed off i parked it up in the garage and havent been in to check on it since.
assuming it is piston failure what sort of money am i looking to rebuild? is it worth anything to sell up and move on? |
You can buy a used long block from mattyb for around 1400
buy a brand new short block for around 1200 go forged from about 3/4k to 10k plus depending on parts used. possibly rebuild yours cheaper but depends on state of the block. just rough prices. |
Cheers for the info mate.
so really even if i want to sell it at the very least im gonna have to put a used long block in? |
Originally Posted by si_pow
(Post 12026998)
Cheers for the info mate.
so really even if i want to sell it at the very least im gonna have to put a used long block in? |
You could sell it as it is,couldn't tell you for how much tho,maybe 1k ish?
|
Originally Posted by the shreksta
(Post 12027000)
yeah but you still need to find out why the original engine has failed. who mapped it?
Op you need to confirm engine failure imo before writing it off. |
Originally Posted by the shreksta
(Post 12027000)
yeah but you still need to find out why the original engine has failed. who mapped it?
the turbo and everything was fitted by cams performance and the remap was done by the guy they use down the road. He came highly recommended so i doubt its an error on their part. i did have a compression check done about 6 months before this happened as i wanted peace of mind and it all come back fine. No leakdown test was done though |
Originally Posted by ossett2k2
(Post 12027002)
chocolate pistons?
Op you need to confirm engine failure imo before writing it off. |
so it blew up whilst cruising on the motorway at 50. Seems odd. Had it been running ok prior to this?
|
Originally Posted by pjarvis6666
(Post 12027163)
so it blew up whilst cruising on the motorway at 50. Seems odd. Had it been running ok prior to this?
|
Actually i do remember i thought it was overboosting. From 3rd gear it nearly went to 1.6bar and having it previously set at 1bar i thought it was too much? Thats why i was driving so careful on the way back as i wanted to ask the opinions of people on here
|
All times are GMT +1. The time now is 03:56 AM. |
© 2024 MH Sub I, LLC dba Internet Brands